Andy@AAV
Well-Known Member
- Thread starter
- #1
I had a plywood and 2x8 temporary solution for almost 3 years so I finally got around to making the real version that had been living in my head. I used 3D printed parts along with some 1x1 aluminum tube and some old airline track I had in the garage. First step was getting the base made, I printed some blocks out that leveled and aligned a piece of square tube where the factory tie-down rings were installed.
Next I made the vertical supports and printed some T-brackets that are bolted through with 8-32 bolts and JB welded in place. The top square tube piece has 1/4-20 threaded inserts that match the hole pattern in the airline track.
Cross supports are 1/2 x 1 aluminum angle that are drilled and countersunk for 8-32 flat heads that are threaded into hammered inserts on the plywood shelf material.
The center support is free floating on the bottom and bolted in place through the airline track.
Last step (almost) was to install everything and find out my 1/4-20 flat heads weren't quite long enough to fully thread into the inserts on the square tube.
Once I got longer bolts everything was test fitted and then I glued/tacked carpet on the plywood so it looks less ghetto...
3 months in and everything is holding up fine after a few trips and 5k miles. I made some 3D printed end caps for the aluminum tubes so it wasn't so sharp. Black parts are printed from carbon-fiber nylon and the blue parts are ASA.
Next I made the vertical supports and printed some T-brackets that are bolted through with 8-32 bolts and JB welded in place. The top square tube piece has 1/4-20 threaded inserts that match the hole pattern in the airline track.
Cross supports are 1/2 x 1 aluminum angle that are drilled and countersunk for 8-32 flat heads that are threaded into hammered inserts on the plywood shelf material.
The center support is free floating on the bottom and bolted in place through the airline track.
Last step (almost) was to install everything and find out my 1/4-20 flat heads weren't quite long enough to fully thread into the inserts on the square tube.
Once I got longer bolts everything was test fitted and then I glued/tacked carpet on the plywood so it looks less ghetto...
3 months in and everything is holding up fine after a few trips and 5k miles. I made some 3D printed end caps for the aluminum tubes so it wasn't so sharp. Black parts are printed from carbon-fiber nylon and the blue parts are ASA.
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